TY - GEN
T1 - Flight testing of a university based H2O2/HDPE hybrid sounding rocket at KAIST
AU - Huh, Jeongmoo
AU - Kim, Youngil
AU - Yun, Yongtae
AU - Ahn, Byeonguk
AU - Kwon, Sejin
AU - Lee, Jaewan
AU - Yoon, Hosung
PY - 2017
Y1 - 2017
N2 - This paper reports results of manufacturing and flight testing of a laboratory scale sounding rocket using a 250 N class hybrid thruster. The propulsion system was configured with a storage tank, tubing lines, and a thruster. 90wt% H2O2 as an oxidizer and high density polyethylene as a fuel grain were used. With catalytic ignition and blow down feeding system, propulsion part could be simply made up. Ground test of propulsion system showed successful combustion using a MnO2/Al2O3 catalyst for catalytic ignition. The sounding rocket was composed of the propulsion system, recovery and flight data acquisition system, and carbon composite casing. Before the flight test, flight trajectory was simulated by developed code considering six degrees of freedom motion showing the reachable altitude of several hundreds of meters. Flight test result showed the propulsion system well functioned without any delay of ignition and the sounding rocket successfully launched. However, the maximum altitude was less than one hundred meter due to the flight direction change affected by a gust of the wind, which indicated the rocket was vulnerable to an aerodynamic disturbance with insufficient initial acceleration and over stably designed fins.
AB - This paper reports results of manufacturing and flight testing of a laboratory scale sounding rocket using a 250 N class hybrid thruster. The propulsion system was configured with a storage tank, tubing lines, and a thruster. 90wt% H2O2 as an oxidizer and high density polyethylene as a fuel grain were used. With catalytic ignition and blow down feeding system, propulsion part could be simply made up. Ground test of propulsion system showed successful combustion using a MnO2/Al2O3 catalyst for catalytic ignition. The sounding rocket was composed of the propulsion system, recovery and flight data acquisition system, and carbon composite casing. Before the flight test, flight trajectory was simulated by developed code considering six degrees of freedom motion showing the reachable altitude of several hundreds of meters. Flight test result showed the propulsion system well functioned without any delay of ignition and the sounding rocket successfully launched. However, the maximum altitude was less than one hundred meter due to the flight direction change affected by a gust of the wind, which indicated the rocket was vulnerable to an aerodynamic disturbance with insufficient initial acceleration and over stably designed fins.
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U2 - 10.2514/6.2017-4901
DO - 10.2514/6.2017-4901
M3 - Conference contribution
AN - SCOPUS:85086059020
SN - 9781624105111
T3 - 53rd AIAA/SAE/ASEE Joint Propulsion Conference, 2017
BT - 53rd AIAA/SAE/ASEE Joint Propulsion Conference, 2017
PB - American Institute of Aeronautics and Astronautics Inc, AIAA
T2 - 53rd AIAA/SAE/ASEE Joint Propulsion Conference, 2017
Y2 - 10 July 2017 through 12 July 2017
ER -